I have just dowloaded the latest SDK and aicraft converter.
The DR400 works fine - no issue.
Then I have tried to convert my MB-326 - restarting from the MB-339 .tmd files...
...ALMOST everything seems to work, but I have an issue: the landing gear now retracts automatically (even with the aircraft on the ground) - and stays retracted.
I could not find the reason why of this behavior.
Also, is there somewhere a list of the changes in the latest aircraft converter?
I think this has nothing to do with the aircraft converter but rather about the changes made to the tmd files.
Those are mainly changes like the logic objects:
For example your landing gear probably has a logic_or for: GearInput.Output OR OnGrounSensor.Output
You need to change this.
On top of this the jointmulti object has been renamed to "multibody_joint" and its "Axis" has been renamed to "X0" and its "Position" to "R0". And there is no longer a need for another jointlinear to create a torque on the jointmulti axis.
There are also other changes
changed logic_or, logic_and, sum and product to input lists (Input0 and Input1 have been merged to one line: "Inputs")
changed auto_spoiler arm logic to support button input
changed auto_brake input logic for rejected takeoff position and added warning output
renamed jointmulti -> multibody_joint
jointmulti.Axis -> multibody_joint.X0
jointmulti.Position -> multibody_joint.R0
added InputLock ? to multibody_joint
added InputPosition to multibody_joint (remove control joints)
I hope this solves your issue with the landing gear.
thanks for you help and the prompt reply.
The MB-326 is back on its landing gear !
Awesome! No problem, you're welcome